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"TURBO INSTALLATION SECTION 7"
This is the last section of the Turbo Install. It contains a cronicle of my trials and tribulations from the completion of the project to date , including some timeslips and event results.
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1/17/01
On 1/17 the first time out at the track only told us that the fuel system
was WAAAAY too fat.The motor did not want to run clear at all down below
5000-6000 rpm's. It was less than a wink of an eye from there to the rev
limiter set at 7800 rpm at which time the motor started poping and farting
from the limiter.The engine did NOT like the MSD rev control when on boost.
So it was back to the shop for some more tuning. After futher experimentation
it was determined the the bleed hole in the poppet of the e-valves were too
large giving the motor excessive fuel at low rpm's. Shrinking them from .046"
to .025" and then enlarging them incrementaly to .036" gave the desired effect.
So back to track for more testing.
2/7/01
On 2/7 I went to another test and tune session. A wet starting line was not
a key ingredient to make a clean pass with a good number.That, combined with
my lack of experience with this motor produced another burnout at the starting
line with the car going HARD left and immeadiately poping on the rev chip.
After lifting late (this ain't nothing like my webers) and settling the car
in the groove, 2nd gear was a repeat of 1st. Finally getting a good squirt
of hooked boosted power in 3rd, it was capped off with more farting on the
chip and a sudden power loss. As the drivers compartment filled with smoke
I had already declutched and flipped the ignition kill switch. Don't you
just hate that sinking feeling in the pit of your stomach ?
Well, it was not as bad as I thought. The #1 cylinder gave up both pushrods.
They both looked like a pair of "~". All else seemed intact and after replacing
them and checking for any other damaged I fired it back up and nothing else
seemed to rear a nasty head. So on 2/11 its back out for another driving
lesson and torture test. Hopefully I can post a time slip from
there.
2/11/01
Well it didn't go as well as planned, but I did get to make one pass under
power untill just after the 1/8 mile cones. After taking out the high side
chip to eleveate all that framing and popping I left the starting line at
4000 rpm's, got a wimpy 60ft and the motor ran very ruff and uneven. Nothing
really started to happen untill the top of second gear and I felt the boost
squirt. I did my best to maintain around 1/4 to 1/2 throttle, and did so,
untill I felt boost in 4th gear and then I matted it.Shorty thereafter both
vale covers huffed heavily with oil. No bent pushrods this pass, but the
oil smoke shyed me into declutching and shuttting down well before the 1000ft
mark.Thats me in the right lane.
2/24/01
Can't seen to stop the popping on boost with any tune-up changes.We have
sorta come to the conclusion that the massive difference in the unequal length
header is fighting us. So now the boost is turned down to 8psi and its back
out to the track. The timeslip below tells a little , but it was one e-ticket
ride. With a medium/hard launch (6000rpm's) the car left and ran clean untill
I shifted into 4th gear when all hell broke loose (literally)in the traction
department. Evidentally, from how my lineman saw it, thats when a large poof
of oil smoke emminated from the car. This is when I went from "racing" to
"skating" and round she goes. At about 80 mph from the looks of the timeslip.
That's when that annoying right gaurdrail got in my way as I tried to back
down the track sideways. Still not sure why the valve covers puked so much
oil, but it was raining under the rear bonnet and both slicks were soaked
in oil when I finally stopped at the 1/8 mph cones. The 1/4 mile and 1000ft
lights were tripped by the rescue truck coming from the big end. Its going
to be a real thrasher to make the North/South Shootout on 3/25 even in
primer.
4/29/01
This was the pass I was sure I was going to get a full on power complete
pass. Boost was down to 7-8 lbs. and I had cured my oiling problems with
the upgrade to my breather system. When I shifted into 4th gear (well before
the 1/8 mile finish line) I heard the fatal crunch-n-munch of my flywheel
separating itself from my scat flanged crank. It had sheared all the cheesy
bolts (i mistakenly used the bolts i got with the used crank from previous
owner) and chewed off all the dowel pins. It was still running as I declutched
(i did not know i was already "declutched") and coasted around to the return
road blipping a curiosly responsive throttle (No flywheel) and vainly trying
to get any gear to pull me back the return road.
5/01/01****UPDATE**** After the attempted
pass at Lakeland the Drag Gods have arranged that I experience the most unusual
thing. With my engine pulled and complete I was tending to my crank flange.
The next morning a large puddle of oil was seen under my motor. Investgation
revealed that some bizzare chemical reaction had taken place inside my motor.
A one inch hole had been eaten through the case from the inside out. Upon
dissasembly a two inch layer of some type of white creamy contaminate was
found floating on top of the oil and every place that contaminate touched
my case there was a similar corrosive reaction. If you have ever seen hydrocloric
acid poured on concrete the etching is very similar with a hole through and
through just above the oil level in one side and similar but slightly less
intense actions all around the oil level line of the inside of the case.
As of yet no one has been able to give me any insight. If you have any input
please forward it to me at Twoghias@aol.com The senerio was as follows:
ENGINE OIL: kendal/used warm up and one 1/8 mile pass
FUEL: methenol with top oil
CASE: as21 stock VW
OTHER POSSIBLE FACTORS: "Transgel" brand red assembly lube had been used
to lube lifters upon assembly
Engine oil was in a state of cronic iron filing contamination from a wiping
cam (evidenced in oberg filter before dissasembly and by actual cam lobes
after dissasembly)
To
view pics of this mystery click here
.
6/01/01***** UPDATE****** I have repaired damaged threads on my crank flange and procured some ARP bolts. I need to enlarge damaged dowel pin holes and install oversized pins to complete crank/flywheel repair. I have a new case,cam,and lifters for reassembly. I i will not be part of Team Magic at Bristol,Tn on 6/8/01, but I will be back at it soon.
8/25/01 ******UPDATE****** OK I havent been here to update for some time. The financial disaster of buying ANOTHER new case gave me a bad attitude and I had to wait for that to come around. As of today the engine is completely installed in Abby and about ready to make smoke. I took the time to remake the header to an equal length system. The old pipes were 14"/27"/30"/45". They are now all 45" long. With 16 feet of header pipe and all the other exhaust and intake tubes it has now gained the nic-name "Frankenpipe". It still fits under the bonnet and I only had to remake 29 other things to get it all to fit.
Hopefully the header mods will bring the tunability of my system around. I still plan on staying at 7 lbs. boost untill I can get a solid history with the way it is now.
9/01/01 ****UPDATE **** Once again it's alive! I am now in the process of tuning her up. Kendrick, my helpfull "Tuner Guru", is on vacation, so I will be stuggling through the new tuneup without him. The initial runs to break in the cam were a struggle to say the least. The barrel valve was seized solid from sitting with old alky in it, so it along with all the jet cans and the injectors had to come apart for a good inspection and cleaning. After addressing a few drips, I found a good starting spot for the more than just sensitive barrel valve setting. By this time my battery was toast and my oil less than desireable. The next tuning session should prep me for the track and a Micky D's pass or two. I can feel the adreniline already starting to build.
9/30/01****UPDATE****The drag gods were smiling and it's about time. Our trip to Darlington, Sc for the North-South Shootout provided me with my first full on pass. 6.74 @105.45 mph. Best of all my tuneup looks good and I experienced no motor issues. There is however some chassis tuning to be done. All but one off my passes at Darlington were in a hard turn begining immeadiately from the starting line. All of the passes were full on the wheelie bars in first, second, and also in third gear if I made it there under hard power before lifting to stay inbounds. My best 60 ft was a 1.42.
10/7/01***UPDATE*** Lakeland dragstrip had a nostalgic race today and a bunch of 4-cylinder races showed up. We were given our own class and raced untill a rainout. Timeslip below tells the story. I had a marvolous time.
Staggering my rear tire pressure by 1 lb. and lowwering it by 4 lbs. really straightened the launch up. My 450 lb. springs on the koni's seem too soft now. The shock snubber traveled all the way to the top off the shock. I have installed 600 lb. springs and raised the wheelie bar support stops by 1-1/2 inches and added a piece of chromemolly tubing in place of all-thread used to make the stops adjustable. The all-thread took a dump on the 6.44 pass. These changes should help keep the leave straight, keep the car front end a lot closer to the ground, and hopefully improve my et. Can you say hauling ass? Sure you can.
10/28/01***UPDATE*** Lakeland dragstrip had the Fisher Buggie race today and I did my best to participate. All seemed well untill I tried to leave the stagging lanes for my first time trial pass. Thats when the Hilborn fuel pump locked up, took out the oilpump/drive adapter, and left me looking "fuelless". No track repair possible here. Maybe next time. However, it was a fabulous day for Oscar in the "Beetle Magic' car. He and his car performed flawlessly to take the win in SuperPro class. Congradulaions to him and thanks for holding up "Team Magic".
1/17/02***UPDATE*** Yep, it has been a while again. I sent my pump to Hilborn for repair and it cost more to fix than a new one. I had to save up $410 for a new fuel pump and find another oil pump. Scat wanted $300 for a single stage oil pump. Fortunately, Tracy Grimm at TG Fabrication hooked me up with a used oil pump from off his dyno at a VERY reasonable price or I would still be saving up. Thanks again Tracy. I am now using an Enderle 80A - #00 fuel pump, as it was a little less than a new Hilborn. The new pump changed the outlet plumbing slightly but basicly bolted on. While I wait for the new race season to start I am doing a little more tuning. The main jet can which usually holds a very light spring and poppet to act as a check valve was modified. I set the main can popppet spring to unseat at 5 lbs. psi (instead of near zero lbs) and this was the most substantial positive change in the motors ability to make a smooth transition from idle. It also has throttle response that previously did not exist. Effects of this change were seen in the fuel pressure gauge (it is installed just before the e-valves) reading which starts up toward 5 lbs. immeadiately as you crack the butterfly. Before this change, system fuel pressure was at zero untill about 3000 rpm's and the motor took some coaxing along to get through the first 2-3000 rpm's. This change also made it necessary to lean out the barrel valve which will help keep oil contamination down. Even though it has been over a year since I first put this system together I am still learning. This is now the best this system has sounded in the shop and hopefully that translates to a best ever et at the track. The first VW event sheduled for this year is in April, but Lakeland Dragstrip has already had one 4-cylinder event and I plan on making the next one they have to finish up my R&D before our first road trip to the Carolina's.
2/2/02***UPDATE*** I sure wish I had 5 grand for a new gearbox because I sure need mo' gear. This was my first attempt at a 1/4 mile track since the car has begun to work. I found out definitively that I only need 660 feet of track, (If I am lucky). Desto Memorial Speedway was today 's site for a test and tune and to try out all my new settings. A few partial throttle launches had me going violently left. Lucky for me JC Quick came along to crew and we made a some wheeliebar and tire pessure changes that concluded in a full on and straight leave. The car was hooking soooo hard that it broke off a 3/4" bolt holding my wheeliebar stop and o-berg oil filter. But , when I got down track I had no traction at all and was breaking the tires loose in 3rd and 4th gear changes. All that throttle pedaling to stay inbounds and off the gaurd rails kept my et a little slow and killed my mph. Best et was a 6.54 @ 95.70 mph. The 60 foot is still 1.42. So .......all I need is less tire at the start, more tire at the big end, and much less boost at the launch or a whole heep of gear in the tranny.
2/9/02***UPDATE*** OK so I don't have 5 grand to build a new gearbox, so I will do what cost little or cost my labor only. The wheelie bars were dismembered today. I took off the two 1-5/8" j-tubes that the bars used to attach to and modified my old wheelie bars to bolt them directly to the brackets off the axels. They are much shorter now, and stiffer. The stops that kept bending or breaking are no longer necessary with the new configuration and they have been removed. Hopefully I can set the wheelie bars very close to the ground and they will still function without taking too much weight off the rear tires. As for the chassis settings, I am going to raise the front of the ladder bar setting to stiffen up the leave and diminish the rotation of the ladder bar winding up the front end off the ground. My #58 turbo exhaust housing is coming off now and I will replace it with a #96. This should be, an easy to find used piece at low buck price. This larger housing will slow the rate at which I build boost and hopefully keep me at little or no boost in 1st gear and still give me a good spank for the rest of the track. If all this works, (I picture all of you laughing hystericly) I may be able to get a little down track traction with a good burnout. I haven't done any tire warming at all (dry, clean off the rocks only) since the car started working too good on the starting line. If I can ever get this bitch to leave correctly BEFORE I break this tranny I going to go racing some day instead of R & D 'ing everytime out.
*** CLICK HERE TO SEE PICTURES FROM
DOWNEY PARK,FL 3/17/02
THE R & S PERFOMANCE CAMP***
4/7/02 ***UPDATE***With only two cars our road trip to the North South Shootout in Darlington SC was a small Team Magic showing. The changes to Abby had mixed results. With the wheelie bar changes I did a waterbox burnout for this event. It has been well over a year since I last did a burnout and my first attemt was a real geek-out. Still the new wheelie bar configuration worked very well. The car left straight and like a rocket with my best 60 ft. time ever, 1.401 The first launch produced a red light (.483) and it was necessary to add a few 1/100th's to my delay box. This was killer, my car is FINALLY working off the starting line. There is still a more chassis work to be done because the car still drifted out of the grove every pass. As for the major engine de-tune change of the exhaust housing, the results was that there was absolutely NO CHANGE in the engine performance. It was like I did not do anything at all in that department. In one way this was good , because I was able to use all the motors power on the leave with the car now leaving straight, but the 3rd and 4th gear changes were still breaking the car loose from the track and I never could make a full on pass. 6.70's was the best I was able to squeeze off with lots and lots of throttle pedaling. Then in first round of eliminations I was insulted once again by a failing fuel pump. This time the pump itself was "hydrualiced" off the oil pump drive adapter. At the top off first gear it was like someone flipped the switch and my day was done. More modifying to be done to the pump drive setup before the 5/5 Fisher race in Lakeland. Oscar did well in the "new" Betlle Magic car showing off all those fresh bright paint colors untill the quater final round.

5/5/02***UPDATE*** The day had been long awaited and I was as prepaired as I have ever been, but illness put me aside for the 5/5/02 Fisher Buggies race in Lakeland. Many other Team Magic members were thrashing in the wings. Noel still had his tranny on the bench the week of the race and Mark Pycke did so many last minute drills he deserves some kind of medal. Oscar steered Beetle Magic into some rounds and Cuco rounded out our racing field. The big show was to be Mark's F.B. Dragster heads up to west coast Paradise Exspress. Mark had been faster with his older Quick Fix but managed a respectable 5.03 and a 4.99 and a 4.96 @ 145mph still struggling with oil control issues. Been there and have the t-shirt Mark. Paradise was a rifle shell and set a new Hot VW's 1/8 mile mph national record at 167 mph. The pass was backed up at 161 mph nearly sawing one into two. Them guys are fast however you spell it or sell it. The biggest news for us was of course Noel's win in the Superpro class. No one could have been more deserving. Cudo's to ya buddy but you will contend with my ass and Abrakadabra next time.
7/7/02***UPDATE*** To day was a 4 cylinder race at Lakeland Dragway. Lots of rotary's and few new fast cars from Puerto Rico. Oscar came along in Bettle Magic and Jerry was racing The Fido Dido sedan. I usally geek-out on my first pass, especially if I have not had any recent seat time. Today was no exception and true to form I super-geeked my first one. I dont think I could have done anything MORE wrong. Twice I tried snapping the wheels to a burnout and both times I bogged the motor. OK. Its my geek-out pass. I go to the line and deep stage. OK. Its my geek-out pass. I let go of my button 2 lights late and pull 1st gear left to the center line. OK. Its my geek-out pass. Then ...I repeat the left turn in 2nd gear, lift, find the center of the track and hammer it. As I cross the finish line I lose my fuel pump, coast to a stop at the end of the return road, and walk back to the pits. I'm thinking...."nice geek-out pass, all uphill from here." Well things did improve. I was able to repair my pump problem and timeslip below tell of some of the fun. The most excitement was my 1st round of eliminations pass. Abby was really shooting straight off the line and I was on another 6.40's pass when I shifted into 3rd gear and the track disapeared from my windshield and it fill with blue. When the wheels came down I was pointed at my opponents door in the other lane. After a momumental save, (i dont know how i did it) I ran over the mph cone and the finish line cone and prepaired to eat the concrete wall to the other side. Somehow, (still dont know how) I missed the wall. I got some minor cone damage, but that kept my heart racing the whole ride home. Oscar went out 1st round swimming in the same spot in the same lane where I lost it on two wheels. Mmmmm.....I'm leaning toward the dirty track excuse too! Jerry did win a round only to be DQ'd for a leaky oil pressure sender. Bummer. More fun next time.
8/11/02***UPDATE*** "The Rock" had their all VW event today in Rockingham, NC and Team Magic was represented by Noel in his Virtual Two car, JC in the K&K car, and myself in Abby. There was about a 25 car field in the money race with lots of trophy racers and a large turnout in the show classes too. My major chassis change ended up with my 3 timetrials being gaurdrail chasing attempts at getting down track. In hind sight, I believe I over compensated in my wheelie-bar adjustment wanting as little wheels up as possible. With only 1/2 " of clearance off the the track surface I think the bars unloaded my rear tires on the squat causing a complete loss of traction after the launch. There also was an issue with my M&H slicks that is still as of yet unresolved. No gumballs of resin were present on the tires when I returned to the pits after my timetrial attempts. This, with the presents of tiny cracks on the tire footprint makes me believe I have roasted all the goodie out these tires and may need new ones. A pass with a wheelie-bar adjustment and a pass on a borrowed set of slicks should tell me where I stand. JC thrashed untill 10:00 pm the day before race day travel with a new motor and also was unable to make elimination rounds. Camshaft blues kept him pitside with me as we watched Noel go to quarter finals losing to a loose injector line causing him not to run his number.
8/18/02***UPDATE*** Another import event at Lakeland Dragway today. This had to be one of the biggest cluster f---s on the planet. Over 3000 spectators and over 300 race cars proved to be more than the promoter had organized for. We arrived at 8:00 am only to be granted one time run before the stagging lanes closed at 2:00 pm. Somehow,(who knows how) first round of eliminations started at 6:00 pm. With one round in, at 8:30pm the rain came to end the event. With over 50 cars in my class alone all 6-second rides or faster, the $12,000 purse was divided into $100 bills for all the remaining cars. Noel and Oscar were both in it too with over 75 cars in their Pro class. My only elimination round pass timeslip is below. It's nothing to be proud of other than I did get the win light. My opponent sure was sleepy at the tree to let me chase the gaurdrail and pedal my 6.97 dial-in to an 8.01 and STILL beat him to the finish line. Notice the margin of victory, .001 seconds. That tells you to NEVER give up on the finish line when your competition is behind you.
9/15/02***UPDATE*** Another import event at Lakeland Dragway today. This event was the smoothest run event at Lakeland ever. Praise the lord for armed security, because that what it took for crowd control. Team Magic had four cars at this event. Buster's rag top and Gil's 73 were in the street class. Oscar's Bug Magic and myself in the super pro class. We all went out second round except for Gil, who braved it untill the third. This was my first outting with the new 9 x 30 tires. 6.65 @ 108mph was the best I could muster, but there are still quit a few adjustments to be made. Wheelie bar height is too high (see pic below, thats the 60 ft. cone in the foreground) and the tire pressure needs a little experimentation. Todays runs were at 8-1/4 psi and I think I will start at 7-1/2 or so next time out. That along with some shock adjustments to try to get some of the bounce out should get some or all of my better et back. The good news is that I didn't have to chase the gaurdrail in any of my 5 passes. I am ready to go play at Darlington on 9/29.
9/29/02***UPDATE*** Team Magic left Orlando with a Six-Pack of cars for the North South Shootout in Darlington. Buster trailered the infamous Mellow Yellow. Donovan brought the Mean Lime Green Machine. Gil flat towed his sedan for the Der Blitz Kafer competition and found out his ride was on the event tee-shirt. Tod's nearly finished but raceable ride made its maiden voyage, and Bettle Magic and Abrakadabra joined in. Edwin brought his 5.90's sedan to try to set a new Hot VW's A/S 1/8 mile record. Edwin pinched a ring on one piston right off the bat (detination from too much timing was the culprit) and even though he and his brother Angel thrashed for 5 hours and made another pass, it was not his day. Buster took 1st place in the inagual event of the DBK point series. This is a new "show and go" competition where looks count but there is a final drag race of the fastest two qualifiers. Tod's first passes in his first time as a drag racer earned him a place of honor in the "No-Lift" club. He had his ride bending the stinger and dragging the apron and stayed in it. I know that wheelie bars are on top of the what to do next list. Oscar went some rounds with Bettle Magic and I lost second round but not before having my share of fun. I didnt get too far with my few chassis changes. The car could not dry spin the tires for a clean off without doing wheelstands in the burnout box. I went down to 7-1/4 lbs. tire pressure but the tires still did not have any wrinkles in the sidewall when it sat on the startline. I turned the leave twostep rpm to 7000 from 6000. When I went to change the shock settings , I found the right side compression was already at the lightest setting. The left side was 2 clicks off the softest setting and the car was going straight so I left those as they were. I did not make any changes to the rebound adjustment, but I lowwered the wheelie bar 1 inch down. This resulted in much lowwer wheelstands with a still much too hard hook. Best 60 foot was a 1.43 slightly better than the previous 1.46 to 1.49. In hindsight, the extra 1000 rpms at the launch probably hurt more than helped. Untill I can get the car to take a "set" and hold it , I probably dont need any more of anything. I am going to lowwer the wheelie bar again next time out, sneek up on slightly lowwer tire pressure, go back to a 6000 rpm leave, and hopefully get the 1.40 (or better) 60 foot I had with the little tires.
Even though the wheelies were low, the car was violently slammed back down on the front wheels and the rear suspension continued to get unloaded several times as I went down track.
10/28/02***UPDATE*** Team Magic showed in force for the Fisher Buggies race at Lakeland. Even though many members were missing we still dominated the small event with winner/runner-up in Superpro, winner in Street, and runner-up in the Pro class. Congrads to Oscar, Jerry, Gil, and Buster. I was fraught with chassis tuning whoas and a on going power loss due to possible issues with my turbo. Next time out I plan on using my "secret weapon" 3 speed gearbox.
Here is the Team Magic lineup for the Fisher Buggies Holloween Classic
11/23/02***UPDATE*** Orlando Speedworld had their annual "Night Of Fire" event today. Five of Team Magic's racers made it to the event. Maiden 1/4 mile race for Hokus Pokus, Kendrick's newly completed supercharged sedan,Oscar in Bettle Magic, Tod in Spellbound, Noel in the LaTony Brothers sedan,and myself in Abrakadabra. The cool air might have been hard on the natives, but the aircooled motors loved temp in the 40's with the air at 800 ft. BELOW sealevel. Several new personal best were set and they can be viewed at the Teams et chart here---->Teams Best ET's . This was my first attempt at a 1/4 mile pass since about 2 years ago when I first built the turbo system. I had built a new wheelie bar, single wheel tripod type, and tried it on my first timetrial pass.
My first pass timeslip above, right lane #4550, I had a terrible leave, much harder than the old wheelie bars. The entire car, all four wheels, actually leaped off the ground TWICE during first gear. I was surprised the tranny wasn't laying on the track in pieces. I was left with one last new thing to try.
On
this pass I tried a second gear start (2.21 gear). The math told me it would
be too tall of a gear but I wanted to try it anyway. As you can see from
the 60ft. it was more than too big and when the clutch pedal dumped, it shut
off the motor with a chirp of the tires. As it stumbled back to life I hammered
the rest of the track and went through the traps right at 8000 rpm's. My
et sucked but the mph was awesome!!!! So much so, that a few people at the
track could not believe it and thought it was some kind of a timing error
glitch.
My first round, and last round , of
eliminations proved to all the naysayers that the timing glitch therory was
wrong. With nothing left to do but a footbrake start, I drove out easy from
the starting line. I had no idea of what to dial-in. The 10.60 I used
was a real wild-ass guess. I had a red-light start (.491) and down the
track I went. Showing no mercy to the motor I went another 1/2 mph faster.
My V-8 opponent must still be scratching his head as to how that VW ran him
down and beat him to the finish line. This was my very first 10 second pass.
Even though the calculated 356 HP at the rear wheels (1550lbs @ 143.26 mph)
and 417 HP at the crank could have made this a 9 second pass (9.51 according
to Gene Berg drag calculator) I was more than thrilled with the ride. It
does not take an Einstien to figure out that my boost was NOT at 9psi.
The math adds up to more like 28 psi. With my current wastegate obviously
unable to control the boost level, a Turbonetics delta-gate style wastegate
is in the works. This season is almost in the bag so I get a few months to
figure something out to get some control back into my starting line violence.
Maybe move the rear shocks to directly over the top of the axels (they are
currently mounted to the rear of them)? Maybe a 3-step rev control with a
micro switch on the shifter actvated to a lowwer rpm in 1st gear only? Maybe
all the above and something else? If you have any ideas, email me, I am open
to any suggestion
12/14/02***UPDATE***

1/12/03***UPDATE*** Fisher Buggies had their first race of the year at Lakeland Dragway today. A few very fast cars from Puerto Rico were there but only about 75 or so cars total. The cold weather , multiple oil downs, and extreme unorganization lead to a mostly bitter day of attemped racing. At 8:00 pm (race started at 8:00 AM!!) when only the second round had been run, all our team racers were glad to be out and ready to go home. I never got past the timetrials due to a broken shock causing me to make violent right turns everytime I pushed the throttle. A 6.701 @ 106.88 was what the new wastegate gave me on the only straight pass. I didn't have an opportunity to view my boost gauge on that pass so I am not sure if I have solved my boost creep problem. The motor sounded much happier at 8000 rpm's than before, like the boost level is less. I actually had the car leave spinning the wheels. 6 lbs of air in the tires, much lowwer wheelie bar setting (went back to the "old" two-wheel bars), and setting the shoch compression up two more clicks, gave a fairly smooth 1.457 60 foot time. I am not sure when or how the one shock got frozen, but it was from then on that the car became almost undrivable. On my last attempt I was almost completely into the other lane and deceided to end my day before my luck ran out. I have a loaner pair of shocks to try but I am leaning toward a new set of "QA-1 Shocks" (formally know as "Hal Shocks"). Repairing the double adjustable Koni's I have cost $600 and I would be left with used rebuilt shocks and $$$ broke! New QA-1's are around $400. Fisher has another race at the end of March but hopefully another chance for more R & D comes up sooner.
2/22/03***UPDATE*** I went with the QA-1 shocks and they are installed. I am using a lowwer spring rate (450 lbs.) instead of the 600 lbs. previously used due to the shock being shorter and requiring me to preload the spring about an inch to get the 10" spring to fit. I will finish the set-up today in prep for an import event tomorrow at Lakeland. Update to be posted soon after.
2/24/03***UPDATE*** I went to the event with high expectations. I was even more thrilled to see track prep work going on before the race. Lakeland is notorious for their "as is" racing. Well that was not enough for some of us. My first and only pass was a straight wheels up leave (1.48 60 foot) with my new shocks. All was well untill the 3rd gear shift and the car wagged so hard I was afraid I was not going to be able to gather it back up. I was lucky and did. Many of the faster cars were unable to make full on passes, yet I saw 3 sub 6 second rides blast down the track. The jury was not completely out untill Ken Fisher made his pass in the Spirit of America roadster. He lost control at about 1/2 track and tried to climb the wall on one side then came off and did 360's untill he smacked the wall on the other side 300 ft. passed the finish line. The sight of his wadded up car took any courage I had left so I loaded up and came home. Another day.
3/6/03***UPDATE*** I was unloading my car after the last event and deceided to do a little playing around in the street. The first street over from my sponsors shop there is a bunch of guys who like playing with rotory motors in small Mazda's, Toyota's, and the like. They drive by our shop sometimes reving their motors and showing off a little too. So when this opportunity arised I couldnt resist going by in Abby and spanking it for them. After an impressive first and second gear blast past their driveway, my tranny popped out of first gear motoring back to the shop. Rut Roh Reorge. Time for a look see. I pulled my motor and torn down the tranny to find a bent 1-2 shift fork and a 1-2 shift rail with a larger than needed slot in the working end. Amazingly that and the pinion nut being loose (30-40 lbs. torque), were the only issues. After 70 plus passes the ring gear and pinion head showed no signs of cracks and all else looked good. I will make the 3/30/03 race at Lakeland.
3/31/03***UPDATE*** The only one making any passes at Lakeland yesterday were the bands of rain that managed to keep the track just damp enough to not be raceable. When the track puddled for the first time I was loaded back up and off to Orlando Speed World to find hopefully better weather. As I entered OSW cars were making passes and it was only 11:30 am. I teched my car right on the trailer, unloaded , then went directly to my lane assignment. This was a national import points race (which I am not involved in due to class regulations that all but exclude vw's) so I was religated to the row of street hondas and yota's in a sportsman bracket class. Ok by me, I just want to make passes and maybe race a little. No sooner than when my lane started to move, the light sprikles came and we were on wait. A short nap and an hour and a half later the track was dry and we started to move the cars again. Well that bubble bursted when I was 2 cars from the waterbox and the sprinkles came again. Finally at 4:00 pm they called the event and I took my TWO rain checks and my car home. It was not ment to be. Next race will be in South Carolina on 4/6. I sure hope it doesn't rain!
4/7/03***UPDATE*** Well if you want God to laugh at you just plan your day. We all checked into the hotel in Florence,SC saturdat afternoon while it was raining. Not a good sign, but on race day morning the Gods were smiling and the weather looked beautiful. The track at Darlington has a noise curfew and no cars can be started untill after 12:00 noon on sundays. So we still had a wait and see kind of outlook at 8:00 am. Time trials started at around 12:30 so I had my turn down the track. Wheels up and straight, a perfect pass untill I missed third gear (remember i have this "first pass is a geek-out thing") 6.80 @ 94 mph. OK, now that I have gotten over that I was up for my second timetrial. With a loud snap, bang, whizz, I left the line turning an immeadiate right. Felt like a broken axel to me. Bummer. After six guys and a floor jack we got my car off the track. Further investigation revealed that I had only broken my u-joint on the right side. These are 1-3/16 inch diameter, solid shaft, 3/4 ton truck u-joints. These are supposed to be "bullet proof " hence no spares are in my race box. Not to worry anyways. An hour later the rain came and we all loaded up for the long trip home.
4/9/03***UPDATE*** I installed TWO (think of them as shoe laces) new u-joints while the car sat on the trailer. It was the only way I could figure to get the car off the trailer without a struggle. This is when I discovered that the right side ladder bar was bent. I removed it and was able to put it back in order with a press. A test drive after the unload told me I might have other issues. There was a very bad washboard feeling when I applied the brakes. After spinning her up on some jackstands it was evident I had bent my rotor when the right wheel and axel tried to leave the car. Some scientific tuning with a dead blow hammer put things back into order. So I am ready for the next event at Lakeland on 4/20 if the weather Gods are willing.
5/12/03***UPDATE*** The sun was shinning and the track was dry on 4/20 at Lakeland. No one else came out so I was flying solo this weekend. With everything seemingly back to working order I kinda started where I left off at. The car was going straight and hooking like gangbusters off the line. I got a 1.41 sixty foot with ALL wheels off the ground at the launch. These were especially violent since I turned the leave 2-step up a 1,000 rpm's. The wheelie bars suffered a bow in both the top rails and the mounting brackets tried to remove themselves. That with a new oil leak from my bellhousing area when I returned pit side gave me a throw in the towel feeling, so I did.
9/28/03***UPDATE*** Darlington, SC was todays race location. With a new flywheel seal and no other real plan we were off racing. Giant wheelstands were the order of the day. I am sure the spectators were impressed, but I had a hard time being pounded all over the track. Other Team Magic racers had a much better day with them finishing in 1st and 2nd in two classes and 2nd in the other class.
10/05/03***UPDATE*** Lakeland,Fl had one of their monthly import events today. I am still leaping completely off the ground in first and sometimes in second gear too. The VW Tranny God sure must be smiling at me because I should have already run over my tranny several times. A few cracks in my exhaust system was letting all my boost out and time trial numbers were slow. Thanks to Ken Fisher for having and lending me his mig welder I was able to patch things up and become competitive. After a few rounds in the quick 16 class the young whippersnapper Noel Latour, (whom won the event) put me on the trailer. I owe him one.
10/12/03***UPDATE*** Farmington, NC has brought the VW's back to the "Farm". The weather sucked in Florida but it was beatiful here for race day. I have lowwered my bottom shock mounts to decamber my rear wheels slightly and gone up a few clicks stiffer on my shocks in an attempt to soften my much too violent leave. I also modified my wheely bar again. First three time trial passes proved I had finally hit the mark on my chassis tuneup. 6.603 6.607 6.600 were the first three timetrial times with the car drilling the center off the track. Wheel stands were inches instead of feet and the car was a dream to drive. Not having to have my kidneys pounded, my arms and feet frailing, and seeing the track during the whole pass, gave me nothing to do but shift down the track. I was killing the tree today with many 5 oh and 5 teen reaction times. The combo proved to be unbeatable and I almost effortlessly went on to the final round and won the event. Next month we will be back in NC racing at Fayettville and we'll see if this was just a fluke or I have finally got a grasp on something.
11/16/03***UPDATE*** Fayettville reminded me that if you want the Drag God to laugh at you, all you have to do is plan your race day. Coming off the high of my win at Farmington did not exsempt me from the racing gremlins. My first pass was a blistering 6.46 et with my best ever 1.37 60 foot time. I am not sure where the tenth and a half appeared from but I was happy. Then I decieded to service my spark plugs and the disaster happened. As I removed #4 spark plug all my threads in the head came with it. Bummer. It took a good hour and a half to find a plug repair insert and a tap. Thrashing to make one more time run before eliminations I hurried to the lanes even though they had closed them in hopes to get a run in. I made it but in my rush I geeked out the launch and blew any chance of getting a relevant number. Not to worry, inspection after the pass in the pits revealed two broken inner valve springs. My day was done.
11/22/03***UPDATE*** The anual Night of Fire was at Speed World tonight. It has been since last years event that I have run a 1/4 mile. A coulpe of broken valve springs needed attending from the Fayetteville Fiasco and I am down to having only a few old and worn used springs in the race box. Repair was easy enough but I couldn't bring myself to turn up my tired motor so I was racing as-is. A few jet changes were necessary to get my best of 10.31 et. I was quickly trailered as soon as eliminations started but did get my fun in.
5/8/04***UPDATE*** My God, has it been that long? I missed the season opener at Darlington,SC in march. I had become weary of trying to massage my poor old race heads into another event. Tired valve springs breaking, spark plug hole stripped, and deminishing seat margins were just for starters. So instead of trying to get the "unobtanium"(head work) done, I opted for the eaisiest, simplist, and most available. I chose CB Performance 044 cnc ported heads. Not too big to be fragile, but big enough. 42 x 37 and pretty much out of the box. My thinking was if these work well enough, repair or replacement will be off the shelf. As with most any single major item change, it was necessary to redo 29 other items to make a happy working unit. Motor was wider with the new heads so push rods, rocker geometry, and exhaust header mods were the begining of needed changes. Old heads (remember these were for a NA application) had 12.2 /1 c/r. The new ones c/r is now 7.0/1 . Aside from the huge 60 cc chambers (remember no extra work out of the box heads) I also changed to a .090" thick head gasket from Clarke Copper Gaskets. These are a hardened gasket and I am hoping to be a much tuffer piece. So now we are going to get above the wastegate spring setting of 9 lbs. and turn up the boost with this much more doable c/r and new heads.
5/17/04***UPDATE*** Fast Times at the Farm was the event name and it sure turned out to be that way. SEVWA hosted the event at Farmington, NC on 5/16 and although its a long trip it cetainly was worth it for me. 19 lbs of boost was what my static check gauge said for my first pass. This produced a 6.47 et @105.99 mph. with a 1.38 60 foot. Not too shabby,but I never really felt the motor working hard. Checking the wastegate setting in the pits did not give me much confidence in my boost controller. It now said 16 lbs. Hmmmmm....so i tried to correct the setting. The controller was just way too sensitive. It is a pressure regulator for a shop compressor and rated at a 160 psi upper working window. I did my best to set it at 23 lbs. Wow!!! That woke it up! 1.35 60 foot and Now the motor was really working. Unfortuately at the top of second gear the the rubber hose on the tube between the turbo and the butterfly was blown out from under the hose clamp and I coasted to the finish. The next time run was a geek out pass and then it happened. 23 lbs of boost and on the wood, Abby screamed a 1.32 60 foot with a 6.200 et @ 110.43 mph. The car was actually going fairly straight with my hands full of minor steering corrections all the way down track. What a blast!! If nothing else that alone was worth the trip. So its now first round of eliminations, I have beaten the Hot VW's national record by .01 seconds and need a back up pass to hold the record. It was not ment to be(at this event) The track officials even gave me one more chance after eliminations with a final time run effort. That produced a 1.34 60 foot with the car wanting that record untill the third gear shift and she fell of the pace and lost power with a 6.73 coasting at 91 mph. Hot damm!!!! hopefully much more of this fun at the Fayetteville, SC race next month.
6/20/04***UPDATE*** Fayetteville ended up in a test of endurance. With a small turnout and great weather I made 8 passes with my best et at a 6.26 @ 110 mph. The 60 foot never came around on the less than perfect track. My best 60 foot of 1.43 was over a tenth off from my last outing. Massive burnouts were the order of the day in a vain attempt to get my short time back. I had some minor damage in the 3rd round when my one wheel wheelie bar snapped my one wheel into two. The bare bar dug the asphalt and then bent up into my header. I was unable to run the number with two holes that were created spilling boost away. A small welding job to renew. All in all was a fun trip. August 1st in Rockingham will be hot but I am looking for great track conditions to boost my efforts.
8/01/04***UPDATE*** This Rockingham event clinched the fact that I needed to have a welder on hand at the track. It also convinced my crewman,(I was already fairly sure), that a budwieser can and circle clamps will not hold up to 25 lbs. boost. Not even a time run today with the first pass losing my exhaust and the other pass a futile attempt.
8/22/04***UPDATE*** With power back on from the storm just in time to leave for Cecil.Ga on the event day morning, I headed out in the wee hours of the morning to make my lone trek to the track. South Georgia Motorsport Park, this almost brand new facility, was a gem. The rest of the R & S crew was surprised to see me already at the track when they arrived from their hotel. Now I had my new portable welder in tow and the only use it got was welding Jerry's muffler back onto his tow vehicle. I pedaled to Quarter finals with 6.30's and 6.40's only to be trailered by the Inch Pincher dragster. I owe him one, and I am sure he knows it.
9/26/04***UPDATE*** WHAT??? Still another himacane. I missed this one at Darlington, SC.
10/24/04***UPDATE*** Back at the Farm in Farmington, NC. I love this track and if anything spectacular was going to happen I wanted it to be here. I squeezed a few more lbs. of boost into the motor (28lbs.) and had a scalded dog leave, 1.35 60 foot, and ran well untill I shifted into 4th gear. That is when the bottom of one of my pistons came off and tried its best to ventilate my case after peppering my head, bending one rod, destroying one cylinder, and breaking my camshaft in two places. I decelerated toward the finish line,decluthed, and the motor locked up, with a 6.26 @ 101 mph. Even though my new welder saw service on the road trip welding Noel's trailer fender back on, it will not help me now.
11/20/04***UPDATE*** I had my motor completed by last weekend and went to our local track "Anual Night of Fire" event in Bithlo, Fl. at Speed World Dragway. There were 400-500 cars with lots of dragsters, exhibition cars, and a ton of door cars. The event ran from 9 am to 3am the NEXT day and they STILL did not finish. It was called due to soooo much dew settling in on the track making it unraceable. Three other VW's from our camp and myself were the only VW's in the event. This is a 1/4 event and I had not made a 1/4 mile pass since this same event last year. My last years best pass was a 10.61 @ 143 mph. Buster was there in Bluebell, his 12 second street rag top. Noel was there with his low 11 second race car. Tod ran a 10.96 in Spellbound. I made my first 9 second pass in Abrakadabra. 9.94 @ 134.50 with my redone motor. Same heads, one resurected cylinder, new eagle rods, while pauter rebuilds my old ones, four new pistons-unnotched, and the same size cam C-85(FK-89) as before. I was running 18 lbs. boost. I turned it down from 28 lbs after the blow up because those new eagle rods made me a little nervous. After repairing ANOTHER broken hockey stick in my tranny during timetrials, I went out first round with a .496 red light. It really did not matter. I was all teeth the whole night.
9/25/05***UPDATE*** I have not updated my pages here for almost the entire 2005 racing season. It's not that I have not raced this season, its more of finding the enthused time to update. I have put only 36 passes on the car since my last postings, but I have made a few worthy accomplishments. Last weekend our local track put on an import race with a quick 16 and pro class. It was touted as a V-8 vs Imports race. The bubble for the import side of the quick ladder was a 5.84 et. Lots of really fast rotaries with one 4.99 et player. So into the pro class I go running 6.40's and wind up the winner in the final round of racing. Even our newest greenhorn racer, Ben Green,(sorry Ben no pun intended), was all teeth as he also went to the final round in the sportsman class. The windfall of the pro class purse paved the way for travel money to my latest race on 9/25 at "The Rock" in Rockingham,NC. This was the bi-anual North vs South all VW shootout with the SEVWA running a race in its point series. I patched a few small holes in the exhaust and turned the boost from 18 lbs. to 20 lbs. Off the trailer it rocketed to a 6.157 @ 113.89 mph. The Hot VW's ASX 1/8 mile record was smashed. It had previously stood at 6.21 for 5 years with Tracy Grimes. Tracy had skidded under the 6.25 et record held for 6 years by my car with its previous owner and builder, Kendrick Roberts. Two 6.25 backup passes to the 6.15 et failed to secure the record back to Abrakadabra and the R & S Performance camp.
10/2/05***UPDATE*** Todd and I went to Jacksonville for an event they were having. Todd'stimeruns were a 7.20 driving all over the track and a 7.10 and a 7.11. Todd somehow made that track actually somewhat work for him but me, thats a different story. First time run was a 6.60 at 12 lbs boost. Then my second timetrial....it was the MOST driving I have EVER done in one pass. I had taken 10 lbs of boost out to start with but that was not really enough. This track was FAAAR from the condition of the Rock. There was grass growing out of the track on each side of the very narrow racing groove in a very narrow track. There was almost no water in the burnout box and the track staff would not let my crewman anywhere onto the track. It was difficult to impossible to do a proper tire warming. From the start line it moved hard left and when I stayed in it and drove back accross the groove it didnt stop jetting right untill I was off the track in the mud. Then the ass end started sweeping back the other way. It was like the energizer bunny when it went to sliding back and forth.......it just kept going and going and going........ and on the last sweep it rolled up onto two wheels. Instead of just tipping over onto the roof, it stop at the very top of the roll (it was on BOTH rims on the drivers side) and then slammed back down onto all four wheels. My car was put onto the trailer while I tried to calm my shakey nerves. Then the race was called a rainout before first round started.
11/06/05***UPDATE*** Today was the 2nd of our VW T-N-T at Orlando Speedworld. All in all 21 air-cooled VW's made their way out to participate in a FREE sponsored day of play. Many personal best efforts were made. First 11 second run for JC Quick and low 12's for Buster. Then I tickeled my best with a 10.01 @ 135mph. Dash plaques were given out and we even had a few awards of our own to pass out.
Winners of the awards were:
Ben Green-"BEST SMELLING INTERIOR"
Tod Latour-"BEST GEARED FOR SPEED"
JC Quick-"LONGEST HIATUS FROM RACING"
6T6Mike-"LARGEST ENTOURAGE"
11/19/05***UPDATE*** I went to our local track last night for their yearly main event. This is about the only 1/4 mile racing I do once a year. Lots of spectators to watch the exihibition jet cars and trucks. So I turned the wick up to 24 lbs. boost and the two step up 600 rpms on the leave.
The 60 foot was way off (my best is 1.28 ). My low gear didnt like the extra hard leave but the increased boost more than made up for it!!!! For the last 100 feet I was popping off of the rev limiter set at 7800 rpms. I need to remove that to see my real mph potential. The event turned into a rain out so that was my only pass. I didnt care, I was all teeth.
4/9/06***UPDATE*** I have
attended one event and a few local outings since my last update. Nothing
of great significance happened. I was unable to make boost at one outing
and took my entire induction system apart looking for the culprit. There
wasn't any smoking gun as to why so I kinda renewed a few things and reassembled.
All new ignition parts, sent out the fuel pump to be flowed, turned my slicks
around, and went out again. I was trying this out at the track a few times
when something exciting happened. I was 'loaned' a T-70 turbo. With the upgrade
install complete, it's off to the track I go. BOTI was putting on an event
at the local track Orlando Speedworld. I had only two attempts at making
a pass that sunday and they both were crapped out. The first attempt, I blew
off a juction hose between the turbo and the butterfly and the second attempt
I ran out of fuel in the pass. What a geek-out day. Boost was turned down
to 16 psi.and both launches were ultra-violent. My wheelie bar was laid flat
and the car road on 6-8 inches of the middle of the bar as witnessed by the
flat spot of the lowwer tube. The bar was also bent up into the rear bonnet
and broke a small hole out in it. This was the same chassis tune-up I used
on the previous setup. On the second pass I had 3/4 lb more air in the slicks
and turned the leave chip down 800 rpm. My lineman said the car squatted
so hard that there was only about 2" of the inner edge of the slick contacting
the track. It left the starting line in a dead hook with zero wheel spin.
I got 1.49 and 1.46 short times[best previously 1.28] with lots of pedaling
in 3rd and 4th gear. Track conditions were very poor. Several early oil downs
and a 20-25 mph cross wind at the big end. There were three crashes with
one guy barrel rolling his ride 6-8 times at the 1000' mark. I will need
to either turn the boost down more or make a major chassis change. I opt
for the latter. To me it's obvious I am making more power at less boost,but
the jury is still out untill I can come up with a full on pass and a time
slip to boot. Heavier springs are on order.
4/22/06***UPDATE*** I have now installed the new springs. Old ones were 10" long and 450 lbs./inch. These were very difficult to install on the QA-1's due to their length. The new springs are only 9" long, but they are 550 lbs./inch rate. I will get out to the track soon to start finding my new chassis tune-up.
8/15/06***UPDATE*** I went ahead and went the whole nine yards before my next attempt with the new turbo. I sent the shocks out to be rebuilt and purchased a new set of M & H slicks. The next outing was at our local track Orlando Speedworld. It is a 1/4 mile track and I was very amped up to make a full on pass with my increased power and new chassis parts and tuneup. This was a local test and tune so track prep was very minimal. I was anxious to get to some of the VHT before any of the street cars ran so I was second in line to make a pass that night. I got quite a bit more excitement than I bargained for. After the 4th gear shift, the motor screamed with its new found power and light up the slicks like a water burnout. I could feel the car raise up in the rear on the now much larger diameter tires. This was at about 135-140 mph at around the 1200 foot mark. Everything after this happened very quickly, but in my mind's eye it seemed like slow motion. The rear of the car continued to rise untill at some point the front end came up with it and the car started a to roll in air with all tires off the ground. I remember thinking, "Not good Mikey, this is NOT good." I was in the right lane and the car moved to the left, rolling and spinning several times on the roof. None of my clan at the starting line could actually count the spins due to the huge debris cloud being thrown up from the track contact. The first major very hard contact was across the track onto the left gaurdrail. At this point I was on my roof going backwards toward the finish line.I remeber looking out the whole were my windshield used to be and saw the starting line tower upsidedown dissapearing as I slided down the gaurdrail. I was STILL hauling butt and thought to myself,"I not hurt, I can't believe I am not hurt, but it's not over yet." The car continued to slide backwards on the roof untill the gaurdrail ended at some point after the finish line. When the rail ended, this let my car start rolling again. It went through a very wide and deep grass ditch and ended up stopped on its wheels trying to back up a steep grass bank. With both hands still on the wheel and my feet at the pedals, I unbuckeled my 5-point, opened my still working door, and stepped out completely unscathed. I looked at my car and wanted to cry. It was pretty much FUBAR'd. Amazingly, somehow, not even one of the wheels/tires comtacted anything during the entire episode. The front and rear bonnet,both fiberglass, had come off early in the wreck and most of the rest of the car body was trashed. It was towed back to my pit rolling and steering smoothly. After bring her home and scrapping the body, the real damage was evedent. The chassis was killed in 4 places. It was not repairable. I have cut it up and discarded it. All the drive train remained intact and unharmed. I stripped the goodies off the car and the rest was thrown away. Abrakadabra lives only as a memory now. Many very good memories indeed. A special thanks to Kendrick Roberts, the chassis builder and welder. Also thanks to Scooter at R & S Performance for making my many years of racing with Abrakadabra possible.
Disclaimer
I am not affiliated with Volkswagen or Volkswagen of America, Inc. or any of its subsidiaries. The word "Volkswagen" and "VW" are registered trademarks and copyrights of VWoA.The use of the words "Volkswagen" , "VW" , or any other "V" words are used merely for descriptive purposes only so please don't sue me. The views expressed on these pages are not necessarily my views or the views of someone else, but are probably similar to your views or the views of someone you know. Items listed as "Bolt on Race" cannot be assembled without extreme modifications. Modifing parts voids all claims and warrentees. All parts are for off road use only. Warrentees are for street driven parts only. All prices can and will be raised without notice. Prices do not include taxes, shipping, handeling, boxing, insurance, or administrative fees. Any damage during shipping voids warrentees. Only "Race Only" parts are available. All items listed as "Race Only" have no warrentees. Misuse, neglect, or intentionally using any product means you void your warrenty. Only origional cartons, unopened may be returned for partial credit of your shipping fees(less taxes,handeling,boxing,and administrative fees), with a 210% restocking fee. Customers have these rights and may also have other rights too but who cares?
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